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![]() | Home > Technical > Possible new turbo?? |
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Yorky Bob Member Since: 28 Apr 2015 Location: Yorkshire Posts: 4561 ![]() ![]() ![]() |
Get the kettle on, make a brew and read.
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proddy Member Since: 22 Sep 2013 Location: Huddersfield Posts: 42 ![]() ![]() ![]() |
Interesting read thanks |
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proddy Member Since: 22 Sep 2013 Location: Huddersfield Posts: 42 ![]() ![]() ![]() |
If anybody has time please listen to these recordings, Exhaust, tick over and underload file you can here a hollow sounding hiss. like air in the system.
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proddy Member Since: 22 Sep 2013 Location: Huddersfield Posts: 42 ![]() ![]() ![]() |
Well this past few days i have replaced all turbo and inter cooler hoses to silicone, blanked off the egr, added another earth from the starter to the battery, changed the fuel filter and air filter. guess what still have the issue!!
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Yorky Bob Member Since: 28 Apr 2015 Location: Yorkshire Posts: 4561 ![]() ![]() ![]() |
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gasman Member Since: 02 May 2013 Location: Tyneside Posts: 914 ![]() ![]() ![]() |
Hi Proddy
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proddy Member Since: 22 Sep 2013 Location: Huddersfield Posts: 42 ![]() ![]() ![]() |
many thanks gasman for your reply.
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gasman Member Since: 02 May 2013 Location: Tyneside Posts: 914 ![]() ![]() ![]() |
Hi Proddy
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Yorky Bob Member Since: 28 Apr 2015 Location: Yorkshire Posts: 4561 ![]() ![]() ![]() |
My 2011 FL2 went up one steep hill in 6th gear loaded up with zest. The current 2013 fairs far worse on the same hill but does give a better mpg return. Somewhere in the process of looking at loss of power it got to be worth ensuring that the software is still performing OK as my own experience is that these engines can vary so much with the way they are set up. FL2 MY10 TD4 GS traded in at 2 years
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daveb500 Member Since: 18 Apr 2016 Location: Tadcaster Posts: 18 ![]() ![]() ![]() |
Proddy after reading through your thread, and seeing you already changed the intercooler hoses, that takes out an idea I had of a boost side air leak, I would double check the hose clamps.
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proddy Member Since: 22 Sep 2013 Location: Huddersfield Posts: 42 ![]() ![]() ![]() |
As promised the final result
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Yorky Bob Member Since: 28 Apr 2015 Location: Yorkshire Posts: 4561 ![]() ![]() ![]() |
Good to get the update.
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proddy Member Since: 22 Sep 2013 Location: Huddersfield Posts: 42 ![]() ![]() ![]() |
That's correct, the arm on the actuator was stiff, this caused the electrics to burn out.
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daveb500 Member Since: 18 Apr 2016 Location: Tadcaster Posts: 18 ![]() ![]() ![]() |
The actuator arm, and vane free up is part of the normal service routine according the service manual. All it involves is removing the actuator from the sensor and then waggling it 10 to 20 times. This makes sure the vanes in the turbo are free from soot and buildup. then reassemble with a high temp grease. Its a pity the dealer you bought the car from hadn't checked the service book. Would have saved you the £1200.
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